Investigation on Improved Optimal Fixed Time Step in Time-History Analysis for Aseismic Design of High-Speed Railway Bridge-Track System

JOURNAL OF EARTHQUAKE ENGINEERING(2024)

引用 0|浏览1
暂无评分
摘要
Time-history analysis is currently the main approach to the aseismic design of high-speed railway, and the time step significantly affects the calculation efficiency and accuracy. A 5-span high-speed railway bridge-track system was used as an example in this study. The effect of different fixed time steps on maximum seismic response was analyzed. An approach of improved optimal fixed time step was proposed by introducing maximum frequency and sampling frequency multiple. According to the research findings, for a specified ground motion record, the calculation error and efficiency of the improved fixed time step decrease with the increasing sampling frequency multiple. For a specified sampling frequency multiple, the calculation efficiency decreases with the increasing high-frequency components in ground motion record. The calculation error of secondary sampling signal for random ground motion records approximately obeys the normal distribution, and a stable and deterministic upper bound can be constructed based on the random sample of calculation error. The sampling frequency of secondary sampling signal in aseismic analysis for high-speed railway bridge-track system should be set as 4f(max). The improved optimal fixed time step should be set as (4f(max))(-1) to simultaneously satisfy both the calculation error and efficiency requirements.
更多
查看译文
关键词
High-speed railway,aseismic design,time-history analysis,time step,calculation error,calculation efficiency
AI 理解论文
溯源树
样例
生成溯源树,研究论文发展脉络
Chat Paper
正在生成论文摘要