谷歌Chrome浏览器插件
订阅小程序
在清言上使用

Performance Study and Analysis of a 300 MW High Backpressure Heat Supply Unit Condenser after Retrofit

PROCEEDINGS OF THE 2ND 2016 INTERNATIONAL CONFERENCE ON SUSTAINABLE DEVELOPMENT (ICSD 2016)(2017)

引用 1|浏览0
暂无评分
摘要
This paper introduces the retrofit of the condenser of a 300 MW high backpressure heating turbine. According to the test data of high and low backpressure situation, we calculated the operation indexes of the condenser at these situation. The condenser terminal temperature difference is both small at high and low backpressure situations, the average condenser terminal temperature difference is 2.09 degrees C and 2.74 degrees C when it's at high and low backpressure situation, which are both are smaller than the design value. After the retrofit, under the normal backpressure condition, the condenser operation pressure is 4.647 kPa at 319 MW load, the condenser pressure is 4.955 kPa after the circulating water flow rate and inlet temperature correction, and the maximum correction terminal temperature difference is 2.15 degrees C, which is slightly higher than the design value. The condenser performance is improved obviously after the high backpressure retrofit. After the retrofit, the condenser pressure at 320 MW conditions is 0.475 kPa lower than 300 MW. Around the load condition of 270 MW, the condenser pressure is 0.416 kPa lower than that before the retrofit.
更多
查看译文
关键词
steam turbine,high backpressure retrofit,condenser retrofit,circulating water heating,performance research
AI 理解论文
溯源树
样例
生成溯源树,研究论文发展脉络
Chat Paper
正在生成论文摘要