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紫檀冲大坝坝顶塌陷分析与处理

Water Resources and Hydropower Engineering(2011)

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Abstract
紫檀冲大坝在劈裂灌浆时发生坝顶塌陷现象,经过分析排除了由于灌浆引起塌陷的原因。根据实地勘察和理论计算得出大坝塌陷的原因是由于大坝心墙内存在沿坝轴线方向的空洞。根据土拱效应理论分析了空洞出现的过程,并提出了解决方案。
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Key words
split-grouting,Zitanchong Dam,dam with narrow clay core,cavity,soil-arch theory,subsidence,settlement of core
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